Sims Bridge
The alarm went off very early for us and we both got up more or less straight away, none of this sitting in bed with our first cuppa this morning! Last time Finesse came out to meet us they arrived just as we’d put the kettle on, I was still getting dressed. But as it turned out we could have had a bit longer with our eyes shut today.
Sims’s bridge isn’t the busiest and it makes a rumbling noise as a car passes over it. A car came over and then soon reversed, that had to be them looking for somewhere to park.
As last time, as soon as they reached us Kris was straight to work inside as Ricky and Chris/Kev were lifting the engine board.
Several months ago we’d noticed a darkening of the oak surround under one of the windows, this had gradually grown into a bigger patch. We’d been instructed to see if we could see anywhere where water might just be getting in around the window, but there was nothing that we could spot. I’ve been cleaning the gutters (for want of a better word) around the window as often as I could hoping that that might help. If it was condensation that was causing it then we’d have had similar happen in the bedroom, but this was the only one.
Nothing for it but to see what was happening underneath all the trim. Kris removed the curtains and then drilled out the wooden plugs that covered the screws on the wood surround. With these undone he lifted the surround away from the window revealing the insulation and structure around the window. Straight away he could see that water was getting in somehow, not lots, just enough to have caused the damage. With no obvious gap or anything to be seen, he cleared away the spray foam around the bottom of the window, still nothing. All the fixings holding the window in were given a turn with an allen key. He then went round the window with some silicon sealant followed by some spray foam to replace the insulation he’d removed. The bottom of this window will now be better insulated than before. Once the foam had expanded he then started to refit the window surround.
What to do about the stain? I have some crystals that when mixed with warm water would bleach the stain, I’ve not tried it, but apparently it works amazingly. Kris had a different idea, he had come prepared with a length of oak precut to fit over the affected wood. This he cut to fit round the Houdini shelf and then stuck it over the top. All staining removed. We decided to do the other end of the same panel so that it looked the same. Job done.
He then moved on to reseal some of the shower and check that all the pipes both in and out weren’t leaking as when we’d had a look behind the pull out shelves we’d noticed a bit of water.
Meanwhile, outside Ricky and Chris/Kev were busy. They removed the temporary batteries that have kept us going for the last year. These were never going to survive our needs for long, but we think that our training on battery management with our shareboat meant that we never ran out of power, we just had to run the engine twice a day.

The new batteries were slotted into the trays that had been made for them so many moons ago and were secured into position. They then made up new cables (bus bars) to connect them, soldering connectors to the ends. The inverter needed some reprogramming now that the type of batteries had changed. Then everything was tested to check it was doing what it should. It was. Hooray!!!! The display panel read 100% charge.

Chris/Kev now moved onto the bow thruster. On our way up to the Ribble last year we had blown a fuse when some weed got caught around the propeller. Mick had hunted round on the internet for replacement fuses. The Vetus ones were around £12 each, but Mick found 200 amp slow blow fuses much cheaper. He ordered several. When they arrived he replaced the fuse, the bow thruster worked for a couple of seconds and then blew the fuse again. Maybe what had caused the problem in the first place was still there. Buying some waders he then got into the water removed the grill and tried to unblock it. There didn’t seem to be anything there. Then in January we hired the dry dock in Chester for a day to see what the problem could be, the tube and prop were clear of any obstruction. Continue reading


With that all done it was time to visit the services. For this you need to pass through one of the 16 moveable bridges on the Gloucester and Sharpness Canal. Many of the bridges are high enough to just cruise straight through, but others are far too low to limbo under. Before we pushed off Mick called the Bridge Keeper at Llanthony Bridge to ask to pass through. We were told to approach and wait for the green light before passing through.

Whilst the water filled, we emptied the yellow water tank and disposed of our rubbish. Mick found an Elsan in the little hut up the ramp next to the bins, so no bushes were going to get a treat from us today.
The new housing estate had plenty of parking, but the towpath was as it looked on Google too high, also Tilly wouldn’t have felt comfortable there. So we carried on.
A call to Hempsted Bridge was made. We could see the Keeper rapidly doing various things on the bridge, then run over to lower the barriers of the off side. Here there are few buttons to press, much of it is done by hand. Once the barriers were down and locked in position he could then wind the bridge open. It took a bit to get going, but once he’d got the momentum up he easily turned the handle. Reaching into a box he turned the lights to green for us to pass. When we were through he did the whole process in reverse to close it, only for a trip boat to want to come through a couple of minutes later. It looks like quite a work out being on Hempsted Bridge.
No such problems at Netherbridge Swing Bridge as there is 14ft 9’’ clearance. This and other high bridges are not manned fulltime as they only need to open when tall ships pass through. Round a couple of bends and the next bridge, Sims Swing Bridge. The light was flashing red and then it turned to green for us to pass even though there was masses of clearance. Just on the other side there was what looked like a gap nearest the bridge for us to pull into. We checked with the keeper that we were allowed to moor there, as long as we were past the bridge lights it was fine. There was sufficient space for us.


We winded nearer the lock, avoiding being anywhere near to the weir and called the Lock Keeper. All the locks on the Severn are manned and a phone call or vhf radio call stirs them into action. We had a short wait for him to set the lock for us with the red flashing light, then once the gates were opening a green arrow pointed us towards the small lock. There are two locks here one small, which we could have shared and a large one, which looks like we’d have fitted in eight times. The large lock is currently closed, but I suspect we’d have been directed to the small one anyway.














The phone call was made at Upper Parting and we were asked how long we thought we’d be. ‘No idea, we’ve never been this way before!’ We were now in a cutting rather than a river, a whole different feel to it. A dart of blue shot across the water top. This is only our second sighting of a Kingfisher since the canals froze, I suspect the lack of water to fish in had an effect on numbers.






Breakfast done and no faffing this morning as we wanted to be away before the blue hire boat. No offence to them, but we didn’t want to be waiting or for them to feel pressured at locks. As we pushed off there was no sign of life from them.

Our run into Worcester was easy, a Viking Afloat boat yesterday had set most of the locks for us, only one had drained overnight. The last two locks down into town were both empty and as I was just starting to fill the top one a chap with a BWML shirt on came and asked if I’d seen a boat. A moving boat, no we’d not seen anyone else moving. He was relieved as I’d saved him quite a walk to try and find it, they must have gone down onto the river.










































By the last few locks we could see that NB Drekely was catching us up, I don’t think we held them up as they hadn’t quite reached the bottom lock as we exited. The Black Prince boat ahead had come down the flight competently, one paddle had been left open a fraction half way down the flight. However their relief was obvious when they’d reached the 30th and final lock of the day, both paddles fully open, I could almost hear their cheers as they ran down towards the pub after closing the gates.



















